by megabite | Nov 9, 2021
DrillScene has been deployed commercially since 2011 and used by leading oil and gas companies around the world. The results from some of these operations are presented here to highlight the value of the DrillScene approach to real-time drilling monitoring. Industry...
by megabite | Nov 9, 2021
Incident DrillScene detected SPP dropping from 209 to 204 bar in 1.5hrs . Wash out alert issued to RTOC. DrillScene + DrillExpect continued to monitor condition Immediate Solution DrillScene trend show SPP continue to drop. Decision taken to POOH. Gas influx while...
by megabite | Nov 9, 2021
Objective NPT Avoidance and optimization by implementation of DrillScene while drilling 17 1/2” x 22” under reaming operation. Solution DrillScene implementation Results DrillScene alerted dropping SPP at 1600hrs vs previous 24hr trend during reaming operation. SPP...
by megabite | Nov 9, 2021
Objective Customer requested Investigative Replay of lost drill string + BHA and subsequent side track incident. Solution DrillScene Replay clearly showed continued washout over 24 hour period whereby traditional RTOC monitoring did not Results DrillScene clearly...
by megabite | Nov 9, 2021
Objective Investigate Replay requested. pack off NPT during POOH. Lost hole section. Symptoms not identified by rig or RTOC. Solution Customer requested ‘Blind Trial’ (with customer WITSML data) with Sekal DrillScene vs existing RTOC service Results DrillScene...